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- April 17, 2017 at 6:46 am #4142JerryParticipant
I have tried this method, “RC low-pass filter circuit to convert PWM signal into an analog voltage”, but I didn’t received proper response from sabertooth. One motor moving very high speed and another motor moving very less speed.
Similar way I have tried with sabertooth in serial mode but there is no positive response.
So return to RC mode, set 1 off, 2 on, 3 on, 4 off, 5 on, 6 off. I will try to write a program in servo style. That may work to solve the problem. But I am not sure, I have a confusion. Can you suggest programmatic changes. If possible kindly provide your contact details. That will help me to interact with you.
If I didn’t use Logic level converter, it will affect Raspberry pi GPIO pins ?
April 11, 2017 at 10:16 am #4121JerryParticipantCan you please tell me exact DIP switch setting ? Whether my program correct or not ? If any problem in my code, can you please tell me what I want to change ?
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